Plugging procedures and suspension of drilling operations for injection well KS-7

dc.contributor.author Puna Geothermal Venture
dc.date.accessioned 2015-07-06T23:50:02Z
dc.date.accessioned 2015-07-07T22:25:33Z
dc.date.available 2015-07-06T23:50:02Z
dc.date.available 2015-07-07T22:25:33Z
dc.date.issued 1991-02
dc.description.abstract "During the drilling of injection well KS-7, the Puna Geothermal Venture has encountered a high temperature, high pressure zone at depth of 1600'. This zone caused the fluid and steam release on the afternoon of February 21, 1991. Since that time the well has been shut in and is being kept in a stable condition by continuous pumping of cold water into the well bore. During this period equipment and personnel were assembled in order to plug the well. PGV is hereby requesting authorization to execute plugging and monitoring operations that we feel are required to bring the well to a stable and safe condition for the long term. This program is described in the attached document and figures."
dc.format.extent 5 pages
dc.identifier.citation Puna Geothermal Venture. 1991. Plugging procedures and suspension of drilling operations for injection well KS-7. Hilo (HI): Puna Geothermal Venture.
dc.identifier.uri http://hdl.handle.net/10524/47995
dc.language.iso en-US
dc.publisher Puna Geothermal Venture
dc.subject injection wells
dc.subject Puna Geothermal Venture
dc.subject KS-7
dc.subject geothermal wells
dc.subject well plugging
dc.subject well abandonments
dc.subject Kapoho
dc.subject Kilauea East Rift Zone
dc.subject Kilauea
dc.subject Puna
dc.subject Big Island
dc.subject Hawaii Island
dc.subject Hawaii
dc.title Plugging procedures and suspension of drilling operations for injection well KS-7
dc.type Plan or blueprint
dc.type Report
dc.type.dcmi Text
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